Making a little progress on the Mustang

Over the past few days, as I’ve gotten the garage cleaned up and organized a little, I’ve also done a few little odds & ends on the Mustang. Nothing major, but I did test the fuel pump and re-install it. I also completely disassembled the distributor, cleaned it up, and ordered parts to finish it. It will need a new lower bushing, points, condenser, primary lead, cap, and rotor. I’m also replacing the drive gear since I’ve replaced the cam.

While I wait for parts to arrive I’ve cleaned everything up, filed off a few casting marks, and so on. The breaker plates seem in really good shape, which is nice since the last Ford distributor I took apart was completely shot. When I’m done it should be as good as new… then I’ll ship it off for re-curve and tuning to match the engine and cam and make it way better than new, if everyone is to be believed.

Tomorrow I’m going to retrieve the exhaust manifolds form storage and get them ready to bolt back on. I’m debating whether to order an intake and carburetor or not. I probably will. Even if the body turns out to be a write-off due to rust, a complete and running, freshly rebuilt engine should be worth more than I have in it at this point. Or the car could be turned into a track toy, but I really doubt I’d take that route. Too much would need to be done to make it in any way competitive in any class.

Hoping to get it to the body shop soon to find out if I’ll be moving forward with the de-rusting or not. Fingers crossed.

A year’s worth of updates

Time flies when you’re ignoring a blog, right? I’ll catch up.

  • The Mercedes is gone. After everything I’d fixed on it, when the transmission decided it didn’t want to work reliably any more — screw it, I was done. It was an awesome car to drive, but not so much fun to own. I replaced it with a much newer 2018 BMW 540i Xdrive, which has been wonderful.
  • Still flying occasionally, but nowhere near as much as I should or want to.
  • Nothing’s happened with the Mustang, other than getting the engine put back together.
  • We’ve picked up a couple more rental houses; that enterprise is going pretty well overall.
  • We switched from Visible to T-Mobile. Visible had great service when we signed up; it slowly degraded to barely usable. TMO has been better, but not great.
  • I just dumped CenturyLink. Our CenturyLink fiber service has been down since Wednesday morning (it’s Friday now). It took me three hours to get through to a human there, on the phone, who told me they could have someone out Saturday morning. Absolutely appalling service. We were up and running on Cox within an hour of leaving the house to go pick up their equipment.
  • Now I remember why I didn’t like Cox’s equipment… zero flexibility, no control over your own local network at all. You can’t even set your own DNS, so my Pi-Hole is not functional. I’ve got new equipment coming this afternoon. New cable modem, router, and mesh wifi.
  • I left my long time employer (a bank) a little over a year ago and now work for another bank.

Oil Pan

Oh, the oil pan… what a mess. Rusty, nasty, covered with road grime, which is a combination of oil that’s been seeping for decades and dirt. Caked on in the corners, throw in a little RTV added over the years by previous owners in an attempt to stop oil seepage. Probably didn’t work, but it sure made a mess of things. Overall it’s not in TOO bad condition, with only one very small dent in the bottom corner that I may try to bump out — but it’s really not an issue.

I used a maroon Scotch-Brite pad and some Jet A (kerosene) to scrub out the flash rust and scorched oil residue from the inside. It looks fairly OK now, I’ll give it one more pass before the final installation. On the outside I tried scraping followed by kerosene and a nylon brush… with limited success. When I got the lip cleaned off enough to not trash the gasket, I temporarily mounted the pan on the bottom of the engine. The bolts — well, they look like what you’d expect of oil pan bolts that were on a ’66 Mustang. Serviceable, but caked with oily grime. But with the oil pan bolted in place, I was able to attack it with a steel bristle welding brush. THAT cleaned things up a lot. There’s more work to be done, but I’d say it’s halfway there now.

After cleaning it up and getting it ready for primer, I’ll pull it back off. The gaskets need a thin coat of Permatex, and maybe a dab of RTV where the gasket sections meet up. Besides that I want to to some de-rusting and cleanup that needs to be done off the block and without the bolts installed. The bolts will get a soak in parts cleaner, followed by a mineral spirits or lacquer thinner rinse. They’ll be fine to reuse.

I have ordered some metal prep, epoxy high temp engine primer, and high temp epoxy Ford blue engine paint from Eastwood. Just for fun I also ordered some paint for the exhaust manifolds. That stuff should be here some time next week. In the mean time I’ll be cleaning up everything that will get painted, then taping and masking everything off. I’m looking forward to buttoning this engine up. I still need to order an intake manifold and carburetor, but I’m going to wait until there are some significant sales going on. I’ve seen 10% and better discounts from Summit Racing before, and I’ll hold off ordering the expensive stuff until that comes around again.

Oh, and I decided not to replace the harmonic balancer. Turns out, there are repair sleeves for just that exact thing. I’ve got some rust dissolver coming to clean it up, and the repair sleeve, so I can keep the original and save about $70. Any time I can restore and use an original part and not buy a new replacement, I consider it a win.

Back to work!!

The Mustang has been sitting for far too long in a state of limbo. Sitting half torn apart, waiting on a couple of connecting rod nuts… then waiting on me to look up torque settings, the list goes on. I need this car finished, and it’s never going to get finished if I don’t do something.

Over the weekend I finished up the cylinder head work. I ported the exhaust ports a while back, and the new intake and exhaust valves have been lapped. I used a bore cleaning brush to run some mineral oil through the valve guide bores, followed by some oil. I got the seals, springs, and keepers installed, followed by the new rocker arms. I temporarily installed the heads, but pulled them off again because I’m missing one dowel pin and didn’t have the head bolts properly lubricated. They’ll go back on tonight, and I’ll adjust the valve lash and lifter preload.

I need all new bolts for the timing cover and water pump. I ordered them from Lowe’s and picked up the bag, only to find that the twit that pulled the order got nearly half of them the wrong size. Of the 16 5/16 bolts I ordered I got an assortment of 1/4, 5/16, and 3/8 bolts. So, I need to go back and return that entire order and just go pull the right bolts myself.

It turns out I’ll need a new harmonic balancer. This one has a definite groove worn from the front seal, plus it’s rusty and really looks like a pain to try to clean up and get reputable looking for a rebuilt engine. So, I’ll order that, plus a Weiand Street Warrior intake manifold. I’m shopping for a carb. Most of the resources tell me that a mild street 289 really only needs about 400-470 CFM. A 600 CFM carburetor is much less expensive and there’s a lot more selection, but I don’t want to over-carb the engine and hurt low end performance, throttle response, and street driveability.

The new oil pump is on the engine, along with its new drive shaft. The pickup is bolted in place, so once I get the timing cover on I’ll be able to mount the oil pan. That will let me pour some oil in the engine and, once the heads and valve train are done, run some oil through the engine and close it up. I can’t re-install it until after the body and front suspension work is done and the engine bay is repainted… but at least I can get it parked out of the way and get to work on the last couple of punch list items on the Mercedes.

More engine progress

Last week I temporarily installed the camshaft, and after a bit of a learning curve got it degreed. I could have saved the effort; the cam reads within half a degree or so of the specs on the cam card. It’s well within my confidence of the measurement process, parallax errors when reading the degree wheel, etc. So, it’s getting installed straight up. The cam is a Summit Racing K3600, which has substantially more lift than the stock cam but not enough to require screw-in studs and the resulting head machine work. Once the cam was checked, I slathered it with the supplied assembly moly lube and re-installed it along with the timing gear and double roller timing chain.

With that done, I went to work on the heads. The stock ’66 289 heads aren’t bad for compression at about 9.3:1. They are not, however, renowned for their excellent flow characteristics to say the least. While this engine was not thermactor equipped, there were large lumps cast into the exhaust ports for air injection. I say there “were“, because they’re gone now. I’d never used a die grinder before, never modified a cylinder head, any of that… but the heads have the thermactor lumps ground out, exhaust ports smoothed as much as I could manage, and I even took the time to gasket-match the ports. I’ll do the same to the exhaust manifolds before re-installing them. I probably removed a pound of cast iron from those heads; what a mess.

Sunday the 5th I got all 8 pistons back in the block, just not torqued yet. And why is that? Because there’s one block, eight pistons, eight connecting rods, eight rod bearings, eight rod caps, and fifteen nuts to secure the rod caps. Where is nut #16? I do not know. My best guess would be, “Somewhere on the garage floor”… although “buried on the workbench” would not be an unreasonable guess either. Sigh. The hunt continues.

As the re-assembly moves on, I’m giving some thought to painting the engine once it’s all back together. One issue is the extreme grime on the oil pan, along with a few other bits. I believe I’m going to gather up the external bits — oil pan, heads, valve covers, timing cover, maybe the exhaust manifolds — and take them to a car wash with a can or two of oven cleaner. I don’t have access to a parts washer or hot tank (which would destroy the timing cover anyway). The valve covers won’t need much since they’re chrome… I’m debating whether to leave them alone or paint them to match. I’ll probably leave them chromed.

Crankshaft back in

Last night I was back in the garage. I decided to check the main bearing clearance. The journals are smooth and measured exactly where they should be. I had never used Plastigauge before, but the concept is pretty basic. Sure enough, the Plastigauge shows about .00125 to just under .002 main bearing clearance.

I applied a generous amount of Lucas assembly lube, which is a thick green lube that looks like it would be pretty good around Halloween. I had to drive the pin out of the rear main bearing to accommodate the new rear main seal. I cleaned up the area with brake cleaner, then plugged the hole with a little silicone gasket compound. I installed the rear main seal and the main bearing caps, tightening them all down to 65 ft-lb.

The Moore rebuilding book says to use silicone on the mating faces of the block and rear main bearing cap. I’m generally not in favor of using silicone sealant anywhere in an engine or fuel system. I have some Permatex Aviation Form-A-Gasket that I considered using, but in the end I used the silicone gasket maker that I had bought for this project. I figured that the amount needed between the cap and block would be so small that it really didn’t matter much what I used, so I wiped on a thin film and tightened the bolts down. I’ll probably re-torque them tonight just to be on the safe side.

I ground the lumps out of the other head; in fact, it’s better than the first one so I’ll have to do a little more on that one. The carbide grinding burrs I bought do an outstanding job of removing iron from castings. I’ll clean them up with a flap wheel later on, but I’m not going to go for a complete polished exhaust port. This is a street engine, and just removing those big lumps of cast iron will do a lot for air flow.

Back to work!

Has it really been two months since I touched this thing? Sheesh. Well, in the mean time I completed the annual condition inspection on the plane, solved a very pesky problem with the Mercedes (turned out to be gummed up fuel injectors, of all things), took a vacation in northern MN, and… umm… whatever.

I gotta get something going with this thing. It’s been taking up way too much space for way too long. I was supposed to have this car done and sold six months ago. But it’s awfully easy to put off things I’ve never done.

Tonight, spurred on by the bravery of a good stout Manhattan, I attacked the heads. It all started innocently enough. I had bought a new dial indicator with a magnetic base to check the valve guides for excessive wear. It was still in the case, so I tried it out. Can you believe I made it to 50-nevermindhowmany years old, grew up the son of a professional mechanical engineer who designed semitrailer tank trucks, and have never used a dial indicator? The valve guides are fine, thank goodness… the worst one I found had .005 wobble at the tip of the valve stem, in any direction. That works out to around .0015 clearance, according to Mr. Monroe’s book. I decided to lap the valves, as long as I was out there.

I got all 16 of the new valves lapped; the seats all look quite good now. While I was at it, I decided to finally try out the carbide burrs I bought a couple months back. One cylinder head now has all four of the big lumps removed from the exhaust ports… THAT was easier than I thought it would be. I’d never used a die grinder as a grinder before, either. I’ve used a cutoff wheel… anyway, I’ll finish the cleanup and polishing (to some degree at least) once the other head is done. I figure even if left rough it will be better than having the big restriction in the port… but I’ll clean and polish them up as best I can. I’m pretty happy with the results.

I was on a roll. I heard a tiny voice taunting me. Took me a while to track it down, but it was the Flex-Hone calling me all kinds of names I won’t repeat here. I swear that’s why I pulled it out of the box of stuff from Summit Racing and doused it with oil. I figured shoving it into a cylinder bore would shut it up. The taunting continued until I had beaten it into submission with a Ryobi drill and a number of passes through the cylinder. By the time I was done the cylinder wall looked so nice, I went ahead and did the other seven. No more taunting from that tool, I tell ya! And those cylinder walls look good now, too. 45 degree cross hatch, and a light coating of WD40 to keep them safe for a few days until they get something better. Like another Jet A cleaning, a light coat of oil, and pistons installed.

While I was out there, I pulled the main bearing caps off and dropped them into the can of degreaser, after removing the old bearings. I used some solvent and a brush to clean up the mating and bearing surfaces in the block, then dropped the new bearing halves into the block and set the crankshaft in place. Figured that was enough for one night, so I went in and spent almost as much time trying to scrub all the grease and iron powder off my hands as I did working on the engine.

Tomorrow I’ll pull those main caps out and try out Plastigauge for the first time, too. I measured the bearing journals with a micrometer early on (I HAVE used those before!), so everything should be OK… but Plastigauge is cheap. If I’m not careful, I may actually have this thing back together before the end of summer. Really, the biggest challenge looks like it will be getting the block and heads cleaned up enough to repaint.

A Mustang update

Heads are off, valve train completely out, everything more or less cleaned up. I sourced all new valves and rockers. The original springs are OK, the free height on all of them measures within spec and within a few thousandths from spring to spring. The cam I’m going to use isn’t too aggressive for the pressed-in factory studs or springs, I don’t think. Once I have the heads cleaned up a little more and check the valve guides with a dial indicator, I’ll start lapping and re-assembling the heads.

The block is ready for honing… but I’m holding off a bit until I figure out exactly what I want to do to clean up the water passages. I’d hate to have to replace the cam bearings, so hot tanking or electrolysis is probably not a good option. I may try some Evapo-Rust or CLR and see how well that works.

Engine progress

It’s been a while since I posted an update, but it’s not like anyone is following this anyway. 🙂 The engine is out, and on the engine stand. I ended up buying a new hoist from Harbor Freight on sale. Getting the engine pulled was relatively easy, especially once we figured out there are bolts holding the flex plate to the torque converter.

The cam and lifters are junk. Lifters are worn completely flat, so they’ve got to go — this was expected. Plus, a new cam should really wake the engine up anyway. No surprises there. Timing chain isn’t too badly worn from what I can see, but that doesn’t matter either since it’s getting replaced.

The heads are off and look about as you’d expect for a 93K-plus mile engine. In my humble opinion, the valves are probably not worth saving. There are grooves worn in the ends. I’m going to look for some GT40 or GT40P heads locally, since they breathe much better anyway. Slightly larger combustion chambers, but not enough to really hurt performance — especially with a new cam that can more than make up for it.

Pistons and bores look great. Cylinder bore wear is .003 or less, except for #5. That one is more like .006, with about .004 taper. Bore, or hone? I don’t know yet. Honing would save several hundred dollars on the cost of the rebuild. The machine shop wants around $300 for a bore & hone. Add to that a couple hundred for new pistons. If I can just hone, then I can re-ring with new moly rings and save close to $500. I’ll do some more measuring and get some expert advice before making a decision. I’m not building a race engine here, so there’s really no need to sink thousands into it.

All of the main and cam bearings look good, no scoring or signs of uneven (tapered) wear. The crank measures within about .001 of spec, so no work needed there assuming it’s not bent – and no reason to suspect it is.

All in all, it looks to be in better shape than I anticipated. It was definitely time for an overhaul, though. I’m sure the valves weren’t opening fully. Given the wear on the lifters and valve stems, I suspect the cam lobes are worn a bit as well. Cylinder walls had no crosshatch left, and there were signs of a little surface rust from sitting for a few years. I think it will benefit greatly from a slightly hotter street cam, better heads, a 4-barrel, and new rings on freshly honed cylinder walls.

More disassambly

Last night I got a little garage time. I pulled one valve cover, just out of curiosity to see what kind of shape things are in. There were no surprises; the engine seems to be in its original condition with 93K miles. I do see evidence that it’s been worked on over the years, of course — blue Permatex everywhere. No clear sign it’s been overhauled though.

I got the carburetor removed, and pulled the intake manifold (a first ever for me). I’m not going further with disassembly until it’s on the engine stand; in fact, I’ll put the valve cover back on to avoid dripping oil when we pull the engine. But, it’s easier now to get to parts of the engine and the various lines that will be disconnected prior to removing it.